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Code Enforcement Detail
Code Enforcement Detail
Case Number CE23110005 complainant  
Case Date 11-02-2023 address  
Origination EMAIL - EMAIL Status C - CLOSED
Operator hlopez Officer CHUCK
Fines Balance $0.00
Lien Balance $0.00
Total Balance $0.00
Property On Case
STRAP NBR A-26-33-28-030-0070-0030 Owner DAVIS ARNOLD ELAINE
Unit   Owner Address 1214 S CAROLINA AVENUE
Property Address 1214 S CAROLINA AVE City/State/Zip AVON PARK FL 33825
City/State/Zip AVON PARK FL 33825 Phone  
Case Description
SOLAR SYSTEM NOT WORKING - (22081708) VISION SOLAR
Inspections/Events Detail
DATETIMEINSPECTION / EVENT TYPEINSTRUCTIONS / COMMENTS
02-19-202401:50 PMREINSPECTIONTHE PV DISCONNECT WAS IN THE OPEN (OFF)
POSITION UPON MY ARRIVAL. PER THE HOME
OWNER, THE PV TECH HAD LEFT IF OFF. I
THEN CHECKED FOR OUTPUT BEFORE PV
STARTUP AND AS EXPECTED, THERE WAS NO
OUTPUT DETECTED. I THEN CLOSED THE PV
DISCONNECT SWITCH AND IN ABOUT 5-10
MINUTES THE SYSTEM CAME ONLINE. OUTPUT
PER LEG WAS IN EXCESS OF 27 AMPS IN
DIRECT SUNLIGHT AND DROPPED AS LOW AS 16
AMPS WHEN SHADED BY CLOUDS. THE METER IS
CONFIGURED FOR NET METERING AND THE
INITIAL VALUES ARE AS FOLLOWS: 01 -
092838 (CONSUMPTION) & 02 - 001576
(PRODUCTION). WHILE I WAS THERE, THE
PRODUCTION SIDE INCREASED TO 001577
CONFIRMING PROPER FUNCTION. I SUGGESTED
THAT THE CUSTOMER SHOULD MONITOR THESE
VALUES DAILY TO CONFIRM CONTINUED
PERFORMANCE, AND TO REQUEST, FROM THE
SOLAR CONTRACTOR, THE PV MONITORING APP
SO THE CUSTOMER COULD HAVE DETAILED
DATA-LOGGING FOR THE SYSTEM.
02-16-202402:21 PMCLOSE COMPLAINTCASE CLOSED BY JKPAYNE
02-16-202401:49 PMCLOSE COMPLAINTCASE CLOSED BY JKPAYNE
11-30-202301:49 PMREINSPECTIONUPON RECEIPT OF ADDITIONAL DATA FROM
SOLAR EDGE, A RECONFIGURATION OF THE
STRING SIZES WILL NOT BE REQUIRED.

UPON SYSTEM COMMISSIONING, REQUEST A
FINAL INSPECTION OF THE SYSTEM TO VERIFY
OPERATION.
11-09-202303:15 PMREINSPECTIONRETURN VISIT AT PROPERTY OWNERS'
REQUEST: INVERTER HAS BEEN REPLACED, BUT
NO ALTERATION OF MODULE STRINGING
PERFORMED. INVERTER WAS ON UPON SITE
VISIT; TURNED OFF PRIOR TO LEAVING.
11-02-202308:40 AMINITIAL INSPECTIONSITE VISIT VERIFIED NO CURRENT OUTPUT
FROM 7.6 KW STRING INVERTER. ALSO
VERIFIED TWO STRINGS OF SIXTEEN 360W
MODULES EACH SUPPLYING DC POWER TO
INVERTER. OPEN CIRCUIT MODULE VOLTAGE
(NOMINAL MODULE OPERATING TEMPERATURE)=
37.9 VDC. 16 X 37.9 = 606.4 VDC. MAXIMUM
INVERTER INPUT VOLTAGE = 480 VDC.

SUSPECT DAMAGE TO INVERTER DUE TO INPUT
OVERVOLTAGE.

REQUIRED ACTION: REPLACE INVERTER;
RECONFIGURE ARRAY STRINGS SO NO MORE
THAN 12 MODULES PER STRING; OBTAIN
PASSED INSPECTION; RELEASE TO DUKE
ENERGY FOR NET METERING.

INITIAL PERMIT #22081708.
11-02-202308:39 AMCREATE COMPLAINTCOMPLAINT RECORDED BY HLOPEZ
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